Snubbing Case History #8

Snubbing Case History #8

Snubbing Case History #8 Objective: Run simple completion string. Well Information: 3,000 Kpa sweet gas well, 580m deep. Procedure: Rig up snubbing unit and pressure test. RIH Snubco tubing end plug, 1 joint, profile, 1.24m pup, and 60 joints. Strip in tubing hanger,...
Snubbing Case History #8

Snubbing Case History #7

Snubbing Case History #7 Objective: Run in the hole simple completion string. Well Information: 4,000 Kpa sweet gas well, 1,400m deep. Procedure: Rig up snubbing unit and pressure test. RIH Snubco Tubing End Plug, BHA and 1,400m tubing, strip in tubing hanger and land...
Snubbing Case History #8

Snubbing Case History #6

Snubbing Case History #6 Objective: Replace 73mm tubing with 60.3mm tubing for better fluid lift, company acquired permission to co-mingle zones, so packer will be removed Well Information: 5,500 Kpa gas well, 1,600m deep. Procedure: Rig up snubbing unit and pressure...
Snubbing Case History #8

Snubbing Case History #5

Snubbing Case History #5 Objective: Remove production tubing to Fracture top zone. Retrieve bridge plug and re-run production tubing. Well Information: 15 Mpa sweet gas well. Depth: 2,200m Procedure: Rig up snubbing unit and pressure test. Come off packer and strip...
Snubbing Case History #8

Snubbing Case History #4

Snubbing Case History #4 Objective: Abandon lower zone and complete upper zones. Well Information: 8,500 Kpa sweet gas well, no longer interest in lower zone. Completion required on upper zones. Depth: 1,450m Procedure: Rig up snubbing unit and pressure test. Come off...