by snubcodev | Aug 6, 2019
Freeze and Hot Tap Case History #3 Objective: Freeze wellhead to remove plunger lift equipment stuck across master valves. Well Information: 8MPa sweet gas well with high LPG production with plunger lift mandrel stuck in top section. Procedure: Remove piping...
by snubcodev | Aug 6, 2019
Freeze and Hot Tap Case History #2 Objective: Freeze wellhead to remove damaged top section. Well Information: 3,700kPa sweet gas well with damaged master valve not allowing access into tubing. Procedure: Warm up wellhead to prevent gel from prematurely freezing....
by snubcodev | Aug 6, 2019
Freeze and Hot Tap Case History #1 Objective: Replace 4 ½” Demco with broken stem. Well Information: Sweet Gas Well Approximately 6000 KPA Procedure: Hold JHA and safety meeting with all personnel. Rig up x/o nipple back to 2” Nitric in 2” x 5K ball valve. Fill valve...