Snubbing Case History #35
Objective: POOH frac string and install production system.
Well Information: 25 Mpa gas well, 2880m deep.
Procedure: Rig up snubbing unit and pressure test. Unset Packer, run in 2 joints and latch onto bridge plug and release. POOH and lay down frac string and BHA. RIH with retrieving tool and tubing, latch onto bridge plug and release. POOH with same. RIH with BHA and production tubing, tag fill. Pull wireline plug, clean out utilizing slim hole valves to TD. Pull 4 joints. Set plug, space out tubing, strip in tubing hanger, land tubing, and rig out snubbing unit.
Time on location: 55 hours over 5 days