Snubbing Case History #9
Objective: Install completion packer and tubing in dual zone gas well.
Well Information: 4,000 Kpa sweet gas well, two producing zones with no authority to co-mingle. Depth: 650m.
Procedure: Rig up snubbing unit and pressure test. RIH Re-entry guide, .6m pup, profile, 3m pup, packer with on/off, 11 joints, blast joints, port sub, pup, and 59 joints. Strip in tubing hanger, set packer, land tubing. Rig out snubbing unit.
Time on location: 4 hours